wheatley
06-21-2010, 06:19 PM
03 evo
built block
Magnus v5
Fatfab 6262
aem ems
e85 with fic 2150's
non cdi cop
Ever since I put this 62 on and turned the boost up I have been having problems with spark blowout. I had only been able to turn it up to 32-34 psi and was going through plugs every few 100 miles. I use a ngk bpr8es gapped to .018 any bigger and it blows spark out sooner.
The other night I wanted to try a known good coil setup as I was beginning to think I had a weak coil on mine. Fathouse was gracious enough for me to barrow his. I wanted to try it with the plugs that were being blown out around 34 psi on my coils. We went out and made a pull, clean. Turned the boost up to 36-37 made a few more pulls and it was clean. Left his house and went out for some pulls. The boost was spiking a little but noting crazy. It was missing out a little at first but got progressively worse as the night went on. By the end of the night I wasn't able to make boost at all without it breaking up. Other than at wot the car didn't seem to have a misfire.
I pulled the plugs last night and here are the pics. Does anyone see anything wrong?
plug 1
http://i13.photobucket.com/albums/a258/mattb16a1civic/plug01.jpg
2
http://i13.photobucket.com/albums/a258/mattb16a1civic/plug04.jpg
3
http://i13.photobucket.com/albums/a258/mattb16a1civic/plug06.jpg
4
http://i13.photobucket.com/albums/a258/mattb16a1civic/plug06.jpg
Last night I put 4 new plugs in at .018 Boost at 37-38. Did a pull to 9k in 3rd gear on Fathouse's coils
6 pulls before a little break up was noticed. I only did one more pull after initial break up and it did it again but worse. Other than wot and right after the break up the car runs and drives fine. Any suggestions guys?
built block
Magnus v5
Fatfab 6262
aem ems
e85 with fic 2150's
non cdi cop
Ever since I put this 62 on and turned the boost up I have been having problems with spark blowout. I had only been able to turn it up to 32-34 psi and was going through plugs every few 100 miles. I use a ngk bpr8es gapped to .018 any bigger and it blows spark out sooner.
The other night I wanted to try a known good coil setup as I was beginning to think I had a weak coil on mine. Fathouse was gracious enough for me to barrow his. I wanted to try it with the plugs that were being blown out around 34 psi on my coils. We went out and made a pull, clean. Turned the boost up to 36-37 made a few more pulls and it was clean. Left his house and went out for some pulls. The boost was spiking a little but noting crazy. It was missing out a little at first but got progressively worse as the night went on. By the end of the night I wasn't able to make boost at all without it breaking up. Other than at wot the car didn't seem to have a misfire.
I pulled the plugs last night and here are the pics. Does anyone see anything wrong?
plug 1
http://i13.photobucket.com/albums/a258/mattb16a1civic/plug01.jpg
2
http://i13.photobucket.com/albums/a258/mattb16a1civic/plug04.jpg
3
http://i13.photobucket.com/albums/a258/mattb16a1civic/plug06.jpg
4
http://i13.photobucket.com/albums/a258/mattb16a1civic/plug06.jpg
Last night I put 4 new plugs in at .018 Boost at 37-38. Did a pull to 9k in 3rd gear on Fathouse's coils
6 pulls before a little break up was noticed. I only did one more pull after initial break up and it did it again but worse. Other than wot and right after the break up the car runs and drives fine. Any suggestions guys?